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As the Solder Flows
Soldering gold connecter pins into through holes can shackle us with further constraints regarding the allowable height of solder fillets up the length of gold pins. Beyond initial manufacture, the rework of these same through hole gold connectors, that is removing and replacing them by hand, is difficult, very difficult.
Like most hand soldering, it used to be easier. Now heavy heat draws and microscopic sizes challenge technician's dexterity, vision and choice of materials. Figure 2 displays a particularly daunting application that showed up at our facility. Not only were the pins gold, the board stacked with heat sucking planes, but the pins were four rows deep. No wonder I'm losing my hair!
Hmmmmmmmmmmm. In order to succeed we had to try something different. The way we saw it, there were four key performance targets:
3. Wetting to the walls of the plated through holes. 4. Maintaining the topside solder fillet below the specified height. To meet these targets (after a good deal of trial and error) a variety of techniques were applied. The key to ensuring the holes properly wet with solder was to accomplish this during the gold pin connector removal step - waiting until the connector re-installation step was too late and would result in a variety of solder flow issues. Utilizing a mini-wave system, the connectors were removed from the board. (See Figure 3) Plated through holes were desoldered with a vacuum desoldering tool. Not your garden variety hand-tool but an AirVac DRS24 Solder Removal tool. (See Figure 4)
Once the connector locations were certified "placement ready" a combination of hand and AirVac convection soldering were used to access the pins. Control of solder volume was essential to ensuring proper fill and preventing improper wicking up the pins. This was accomplished at challenging locations by adding pre-manufactured "solder donuts" (see Figure 5).
All-in-all a pretty time consuming process, but sometimes that's what it takes to be successful in rework. As you can see from Figure 6, the time was well spend and the results were pretty darn good.
Several members of the Circuit Technology Center team contributed to this feature story. |
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CircuitMedic